富水煤系地层隧道仰拱隆起原因分析及控制研究

On the Causes and the Control Measures of the Tunnel Inverted Arch Heaving in Water-rich Coal Measure Strata

  • 摘要: 贵州某隧道穿越高水压煤系地层时,多处出现仰拱隆起问题。通过现场观察和衬砌结构变形监测,并采用数值模拟方法对隧道仰拱隆起的原因进行分析。结果表明,基底围岩软化和高水压力是隧道仰拱隆起的两大因素,且围岩软化对仰拱结构安全的影响更大。结合工程特点和病害成因,现场采用增设边墙卸水孔、横纵向排水管加强排水系统来减小水压,在拱脚施作注浆钢花管来加固基底围岩以及换拱等联合整治措施,取得了良好的整治效果。

     

    Abstract: When a tunnel in Guizhou passed through the coal measure strata with high water pressure during con? struction, it encountered the problem of the inverted arch heaving. This paper analyzes the causes of the tunnel inverted arch heaving through on-site observation and monitoring of the lining structure deformation, combined with numerical simulation. The results show that the rock softening at the base and high water pressure are the two main factors for the heaving of the tunnel inverted arch, and the former has a greater impact on the safety of the inverted arch structure. Combined with the engineering characteristics and the causes of the disease, comprehensive remediation measures are taken at the site, such as installing additional discharge holes at sidewalls, horizontal and vertical drain pipes to strengthen the drainage system and reduce the water pressure, installing perforated grouting pipes at the arch foot to strengthen the bedrock at the base and replacing the arch structure, etc., achieving good remediation results.

     

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