富水复合地层土压平衡盾构渣土改良试验研究

Experimental Study on the Muck Improvement of Earth Pressure Balance Shield Tunnelling in Water-bearing Composite Stratum

  • 摘要: 针对南昌地铁4号线富水复合地层,对饱和砾砂和中风化泥质粉砂岩进行渣土改良试验,选择合适的改良剂,并开展改良剂性能测试,基于坍落度试验、渗透性试验、直剪试验确定饱和砾砂和中风化泥质粉砂岩的改良剂合理添加比。将室内渣土试验成果应用于现场渣土改良,验证室内渣土改良试验的合理性。结果表明,采用泡沫剂溶液浓度为3%和膨润土泥浆配合比为1∶8时,改良剂性能满足工程要求。对于饱和砾砂渣土,合适的改良剂添加方式为泡沫与膨润土泥浆比4∶1,添加比为5%~7%;对于中风化泥质粉砂岩,合适的改良剂添加方式为泡沫与膨润土泥浆比为1∶4,添加比为10.8%~12.6%,或者全膨润土泥浆,添加比为9.9%~12%。

     

    Abstract: In view of the water-bearing composite stratum of Nanchang Metro Line 4, a muck improvement test has been conducted on saturated gravelly sand and moderately weathered argillaceous siltstone, and the appropriate modifier is selected and the performance test of the modifier is carried out. Based on the slump test, permeability test and direct shear test, the reasonable addition ratio of the modifier for saturated gravel sand and moderately weathered argillaceous siltstone are determined. The indoor muck test results are applied to the on-site muck improvement to verify the rationality of the indoor muck improvement test. The results show that the performance of the modifier meets the engineering requirements when the concentration of foam agent solution is 3% and the bentonite slurry ratio is 1∶8. For saturated gravelly sand muck, the proper addition method of modifier is that the ratio of foam to bentonite slurry is 4∶1, and the addition ratio is 5%~7%. For moderately weathered argillaceous siltstone, the proper addition method of modifier is that the ratio of foam to bentonite slurry is 1∶4, the addition ratio is 10.8%~12.6%, or the addition ratio of full bentonite slurry is 9.9%~12%.

     

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